| P0219 |
Engine Overspeed Condition |
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- range position not P, R, N
- range position not P, R, N
- engine speed no error detected
- time since range position not P, R, N 2 s
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| P060A |
Internal Control Module Monitoring Processor Performance |
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| P060B |
Internal Control Module A/D Processing Performance |
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| P0603 |
Internal Control Module Keep Alive Memory (KAM) Error |
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| P0605 |
Internal Control Module Read Only Memory (ROM) Error |
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OR
- SW verify of EEPROM emulation negative
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| P0607 |
Control Module Performance |
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- SW functions actuating solenoid valves colliding of 2 substitute functions same priority driven solenoid valves have short circuit to supply or interruption
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| P060A |
Internal Control Module Monitoring Processor Performance |
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- CAN Bus no error detected
- CAN Level no error detected
- ignition On
- battery voltage > 9 V
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| P0614 |
ECM/TCM Incompatible |
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- CAN level engine does not fit to CAN level transmission
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- CAN Bus no error and ready to transmit
- ignition On
- ECM no timeout
- output speed < 75 RPM
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| P0634 |
Control Module Internal Temperature "A" Too High |
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TCU SHUTOFF AT HIGH TEMPERATURE:
- transm. oil temp. OR chip temperature (dependent on battery voltage) >= [ 16.55; 18.62; 19.65; 21] [ 141; 121; 111; 61] °C
- characteristic description [x1;x2; - ] [y1;y2; - ]: x: input value in V, y: output value in °C
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| P0641 |
Sensor Reference Voltage "A" Circuit/Open |
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- sensor supply voltage too high > 10 V
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- battery voltage > 6.51 + 1.3 V
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| P0642 |
Sensor Reference Voltage "A" Circuit Low |
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- sensor supply voltage too low < 6.51 V
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- battery voltage > 6.51 + 1.3 V
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| P0705 |
Transmission Range Sensor "A" Circuit (PRNDL Input) |
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- signal line L3/L4 diagnosis by ASIC
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- sensor supply 6.51 < - < 10 V
- sensor supply no error detected
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| P0706 |
Transmission Range Sensor "A" Circuit (PRNDL Input) |
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- 4 bit position code incorrect
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- sensor supply 6.51 < - < 10 V
- sensor supply no error detected
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| P0707 |
Transmission Range Sensor "A" Circuit Low |
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- signal line L3/L4 diagnosis by ASIC
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- sensor supply 6.51 < - < 10 V
- sensor supply no error detected
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| P0708 |
Transmission Range Sensor "A" Circuit High |
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- signal line L3/L4 diagnosis by ASIC
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- sensor supply 6.51 < - < 10 V
- sensor supply no error detected
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| P0710 |
Transmission Fluid Temperature Sensor "A" Circuit |
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SENSOR SHORT CIRCUIT:
- U_sensor + - U_sensor - < 0.9 V
- and U_sensor - < 2.7 V
- U_sensor + > 2.3 V
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- no failure detected in other Transm. Oil Temp. Monitors
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WEAK SHORT-CIRCUIT:
- U_sensor_plus + U_sensor_minus < 0.9 * 5 V
- or U_sensor_plus + U_sensor_minus > 1.1 * 5 V
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| P0711 |
Transmission Fluid Temperature Sensor "A" Circuit Range/Performance |
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HIGH SENSOR RESISTANCE:
- U_sensor_plus - U_sensor_minus > 2.8 V
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- no failure detected in other Transm. Oil Temp. Monitors
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PLAUSIBILITY TO SUBSTRATE TEMPERATURE:
- absolute difference between oil temperature and chip temperature in thermodynamical stable condition > 20° C
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- absolute difference between oil temperature and chip temperature in thermodynamical stable condition 25 or 30° C
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- temperature fault no other fault detected
- chip temperature no error detected
- engine speed or input speed > 400 RPM
- and signal status no error detected
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| P0712 |
Transmission Fluid Temperature Sensor "A" Circuit Low |
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- circuit low U_sensor - < 0.5 V
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- no failure detected in other Transm. Oil Temp. Monitors
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| P0713 |
Transmission Fluid Temperature Sensor "A" Circuit High |
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- circuit high U_sensor + > 4.5 V
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- no failure detected in other Transm. Oil Temp. Monitors
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| P0714 |
Transmission Fluid Temperature Sensor "A" Circuit Intermittent |
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OPEN CIRCUIT:
- U_sensor + > 4.5 V
- and U_sensor - < 0.5 V
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- no failure detected in other Transm. Oil Temp. Monitors
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| P0716 |
Input/Turbine Shaft Speed Sensor "A" Circuit Range/Performance |
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- signal higher or lower than threshold >= 8000 RPM or < 20 RPM
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- sensor supply no error detected
- sensor no electrical error
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- sensor supply no error detected
- engine speed > 600 [RPM
- status engine speed no error detected
- output speed > 500 RPM
- status output speed no error detected or Substitute value
- range position no error detected or Substitute value
- sensor no electrical error
- transmission condition friction-locked
- error flag fnabvra_Err not set
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| P0717 |
Input/Turbine Shaft Speed Sensor "A" Circuit No Signal |
OR
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- sensor supply no error detected
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| P0721 |
Output Shaft Speed Sensor Circuit Range/Performance |
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- signal > threshold > 10000 RPM
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- sensor supply no error detected
- sensor no electrical error
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- difference between last and actual value > threshold -1000 RPM
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- transmission condition friction locked
- input speed sensor no error detected
- difference (converted output speed, input speed) > 200 RPM
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- difference to wheel speeds > 500 RPM and input speed > 200 RPM
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- transmission condition friction locked backwards or forwards
- shift flag = 0 (no shift)
- input speed no error detected
- sensor supply no error detected
- wheel speeds no error detected
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| P0722 |
Output Shaft Speed Sensor Circuit No Signal |
OR
OR
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- sensor supply no error detected
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| P0727 |
Engine Speed Input Circuit No Signal |
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- CAN message signal error flag = 1
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- ignition On
- CAN Bus no error detected
- ECM CAN connection no error detected
- battery voltage > 9 V
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| P0730 |
Incorrect Gear Ratio |
Ratio Engagement Nx -> 1 |
DURING GEAR-ENGAGEMENT IN PROCESS:
- if start-ratio >= target-ratio)
- (input-speed / output-speed) > (start-ratio + 30)
- or (input-speed / output-speed) < (target-ratio - ([ 50; 70; 200; 300; 420; 600; 850; 1200] [ 0; 0.71; 3.16; 3.52; 3.7; 3.84; 3.935; 4.005] + 32.767))
- if start-ratio < target-ratio
- (input-speed / output-speed) < (start-ratio - 32.767)
- or (input-speed / output-speed) > (target-ratio + ([ 50; 75; 120; 200; 330; 520; 800; 1200] [ 12.44; 9.09; 6.74; 5.16; 4.77; 4.56; 4.42; 4.335] + 30)
- input-speed (old) - input-speed (actual) < 40 RPM
- or input-speed (old) - input-speed (actual) > -40 RPM
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- detection active during gear-engagement (active = 1)
- if output speed >= 50 RPM
- if output speed < 50 RPM
- timer < 1.5 s
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- 3 failed rationality checks
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| P0730 |
Incorrect Gear Ratio |
Ratio Engagement Nx -> 2 |
- if start-ratio >= target-ratio
- (input-speed / output-speed) > (start-ratio + 25)
- or (input-speed / output-speed) < (target-ratio - ([ 140; 200; 360; 570; 870; 1200; 1700; 2300] [ 0; 1.38; 1.79; 2; 2.11; 2.175; 2.222; 2.252] + 32.767))
- if start-ratio < target-ratio
- (input-speed / output-speed) < (start-ratio - 32.767)
- or (input-speed / output-speed) > (target-ratio + ([ 50; 110; 200; 360; 630; 1000; 1500; 2300] [ 9.64; 5.27; 3.32; 2.9; 2.65; 2.54; 2.475; 2.427] + 25))
- input-speed (old) - input-speed (actual) < 40 RPM
- or input-speed (old) - input-speed (actual) > -40 RPM
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- timer < 0.5 s
- detection active during gear-engagement (active = 1)
- if output speed >= 50 RPM
- if output speed < 50 RPM
- timer < 1.5 s
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- 3 failed rationality checks
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| P0730 |
Incorrect Gear Ratio |
Ratio Engagement Nx -> 3 |
DURING GEAR-ENGAGEMENT IN PROCESS:
- if start-ratio >= target-ratio
- (input-speed / output-speed) > (start-ratio + 30)
- or (input-speed / output-speed) < (target-ratio - ([ 180; 200; 380; 650; 1100; 1700; 2500; 3500] [ 0; 0.58; 1; 1.22; 1.34; 1.405; 1.442; 1.465] + 32.767))
- if start-ratio < target-ratio
- (input-speed / output-speed) < (start-ratio - 32.767)
- or (input-speed / output-speed) > (target-ratio + ([ 50; 115; 200; 380; 620; 1100; 1900; 3500] [ 8.64; 4.15; 2.45; 2.05; 1.84; 1.705; 1.625; 1.578] + 30))
- input-speed (old) - input-speed (actual) < 40 RPM
- or input-speed (old) - input-speed (actual) > -40 RPM
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- timer < 0.5 s
- detection active during gear-engagement (active = 1)
- if output speed >= 50 RPM
- if output speed < 50 RPM
- timer < 1.5 s
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- 3 failed rationality checks
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| P0730 |
Incorrect Gear Ratio |
Ratio Downshift 3 -> 1 |
DURING GEAR-SHIFT IN PROCESS:
- (input-speed / output-speed) > (start-ratio + ([ 180; 200; 380; 650; 1100; 1700; 2500; 3500] [ 0; 0.58; 1; 1.22; 1.34; 1.405; 1.442; 1.465] + [ 160; 200; 500; 700; 1000; 1500; 2000; 2400] [ 0; 0.9; 0.9; 0.82; 0.58; 0.39; 0.29; 0.25]))
- and (input-speed / output-speed) < (target-ratio - ([ 180; 290; 500; 800; 1300; 2000; 2800; 4300] [ 0; 0.47; 0.74; 0.895; 0.99; 1.04; 1.072; 1.096] + [ 700; 1000; 1500; 2000; 2500; 3000; 4000; 5000] [ 0.14; 0.15; 0.2; 0.2; 0.18; 0.17;0.145; 0.12]))
- no monitoring
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- timer < 0.5 s
- if output speed >= 50 RPM
- if output speed < 50 RPM
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- 3 failed rationality checks
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| P0730 |
Incorrect Gear Ratio |
Ratio Engagement Nx -> 4 |
DURING GEAR-ENGAGEMENT IN PROCESS:
- if start-ratio >= target-ratio
- (input-speed / output-speed) > (start-ratio + 15)
- or (input-speed / output-speed) < (target-ratio - ([ 180; 290; 500; 800; 1300; 2000; 2800; 4300] [ 0; 0.47; 0.74; 0.895; 0.99; 1.04; 1.072; 1.096] + 32.767))
- if start-ratio < target-ratio
- (input-speed / output-speed) < (start-ratio - 32.767)
- or (input-speed / output-speed) > (target-ratio + ([ 50; 100; 200; 370; 650; 1200; 2300; 4300] [ 8.52; 4.02; 2.12; 1.68; 1.45; 1.305; 1.23; 1.189] + 15))
- input-speed (old) - input-speed (actual) < 40 RPM
- or input-speed (old) - input-speed (actual) > -40 RPM
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- timer < 0.5 s
- detection active during gear-engagement (active = 1)
- if output speed >= 50 RPM
- if output speed < 50 RPM
- timer < 1.5 s
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- 3 failed rationality checks
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| P0730 |
Incorrect Gear Ratio |
Ratio Downshift 4 -> 2 |
DURING GEAR-SHIFT IN PROCESS:
- (input-speed / output-speed) > (start-ratio + ([ 180; 290; 500; 800; 1300; 2000; 2800; 4300] [ 0; 0.47; 0.74; 0.895; 0.99; 1.04; 1.072; 1.096] + [ 300; 500; 700; 1000; 1200; 1600; 2000; 3000] [ 0.45; 0.52; 0.65; 0.58; 0.5; 0.39;0.31; 0.21]))
- and (input-speed / output-speed) < (target-ratio - ([ 50; 110; 200; 360; 630; 1000; 1500; 2300] [ 9.64; 5.27; 3.32; 2.9; 2.65; 2.54; 2.475; 2.427] + [ 50; 80; 140; 300; 500; 1000; 1800; 3000] [ 12; 7; 5; 0.88; 0.5; 0.24; 0.11; 0.045]))
- no monitoring
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- timer < 0.5 s
- if output speed >= 50 RPM
- if output speed < 50 RPM
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- 3 failed rationality checks
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| P0730 |
Incorrect Gear Ratio |
Ratio Engagement Nx -> 5 |
DURING GEAR-ENGAGEMENT IN PROCESS:
- if start-ratio >= target-ratio
- (input-speed / output-speed) > (start-ratio + 15)
- or (input-speed / output-speed) < (target-ratio - ([ 220; 350; 600; 1000; 1500; 2300; 3500; 5000] [ 0; 0.31; 0.55; 0.67; 0.735; 0.78; 0.81; 0.828] + 32.767))
- if start-ratio < target-ratio
- (input-speed / output-speed) < (start-ratio - 32.767)
- or (input-speed / output-speed) > (target-ratio + ([ 50; 100; 200; 400; 750; 1400; 2700; 5000] [ 8.71; 3.75; 1.82; 1.36; 1.13; 1.007; 0.94; 0.907] + 15))
- input-speed (old) - input-speed (actual) < 40 RPM
- or input-speed (old) - input-speed (actual) > -40 RPM
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- timer < 0.5 s
- detection active during gear-engagement (active = 1)
- if output speed >= 50 RPM
- if output speed < 50 RPM
- timer < 1.5 s
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- 3 failed rationality checks
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| P0730 |
Incorrect Gear Ratio |
Ratio Downshift 5 -> 3 |
DURING GEAR-SHIFT IN PROCESS:
- (input-speed / output-speed) > (start-ratio + ([ 220; 350; 600; 1000; 1500; 2300; 3500; 5000] [ 0; 0.31; 0.55; 0.67; 0.735; 0.78; 0.81; 0.828] + [ 700; 1000; 1500; 2000; 2500; 3000; 4000; 5000] [ 0.4; 0.52; 0.395; 0.31; 0.255;0.225; 0.18; 0.15]))
- and (input-speed / output-speed) < (target-ratio - ([ 50; 115; 200; 380; 620; 1100; 1900; 3500] [ 8.64; 4.15; 2.45; 2.05; 1.84; 1.705; 1.625; 1.578] + [ 50; 400; 700; 1000; 1500; 2000; 3000; 5000] [ 7; 1.5; 0.7; 0.4; 0.25; 0.2; 0.13;0.06]))
- no monitoring
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- timer < 0.5 s
- if output speed >= 50 RPM
- if output speed < 50 RPM
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- 3 failed rationality checks
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| P0730 |
Incorrect Gear Ratio |
Ratio Downshift 6 -> 4 |
DURING GEAR-SHIFT IN PROCESS:
- (input-speed / output-speed) > (start-ratio + ([ 300; 380; 500; 750; 1300; 2200; 3700; 6000] [ 0; 0.19; 0.29; 0.43; 0.54; 0.602; 0.638; 0.658] + [ 1100; 1500; 1750; 2000; 3000; 4000; 5000; 6000] [ 0.3; 0.38; 0.33; 0.29; 0.2; 0.15; 0.12; 0.095]))
- and (input-speed / output-speed) < (target-ratio - ([ 50; 100; 200; 370; 650; 1200; 2300; 4300] [ 8.52; 4.02; 2.12; 1.68; 1.45; 1.305; 1.23; 1.189] + [ 50; 500; 900; 1500; 2000; 3000; 5000; 6000] [ 7.5; 0.5; 0.26; 0.15; 0.11; 0.07; 0.04; 0.02]))
- no monitoring
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- timer < 0.5 s
- if output speed >= 50 RPM
- if output speed < 50 RPM
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- 3 failed rationality checks
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| P0730 |
Incorrect Gear Ratio |
Ratio Engagement Nx -> 6 |
DURING GEAR-ENGAGEMENT IN PROCESS:
- if start-ratio >= target-ratio
- (input-speed / output-speed) > (start-ratio + 15)
- or (input-speed / output-speed) < (target-ratio - ([ 300; 380; 500; 750; 1300; 2200; 3700; 6000] [ 0; 0.19; 0.29; 0.43; 0.54; 0.602; 0.638; 0.658] + 32.767))
- if start-ratio < target-ratio
- (input-speed / output-speed) < (start-ratio - 32.767)
- or (input-speed / output-speed) > (target-ratio + ([ 50; 200; 340; 600; 1000; 1800; 3300; 6000] [ 7.74; 1.68; 1.27; 1.03; 0.885; 0.8; 0.752; 0.724] + 15))
- input-speed (old) - input-speed (actual) < 40 RPM
- or input-speed (old) - input-speed (actual) > -40 RPM
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- timer < 0.5 s
- detection active during gear-engagement (active = 1)
- if output speed >= 50 RPM
- if output speed < 50 RPM
- timer < 1.5 s
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- 3 failed rationality checks
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| P0730 |
Incorrect Gear Ratio |
Ratio Engagement Nx -> R |
DURING GEAR-ENGAGEMENT IN PROCESS:
- if start-ratio >= target-ratio
- (input-speed / output-speed) > (start-ratio + 30)
- or (input-speed / output-speed) < (target-ratio - ([ 50; 80; 190; 330; 500; 700; 1000; 1500] [ 0; 0.9; 2.36; 2.8; 3.01; 3.12; 3.205; 3.27] + 23))
- if start-ratio < target-ratio
- (input-speed / output-speed) < (start-ratio - 23)
- or (input-speed / output-speed) > (target-ratio + ([ 50; 115; 200; 330; 540; 700; 1000; 1500] [ 10.24; 6.64; 4.37; 4; 3.77; 3.7; 3.6; 3.535] + 30))
- input-speed (old) - input-speed (actual) < 40 RPM
- or input-speed (old) - input-speed (actual) > -40 RPM
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- timer < 0.5 s
- detection active during gear-engagement (active = 1)
- if output speed >= 50 RPM
- if output speed < 50 RPM
- timer < 1.5 s
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- 3 failed rationality checks
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| P0741 |
Torque Converter Clutch Circuit Performance/Stuck Off |
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- rate of (setting of nominal value) - actual value
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- status of clutch closed or closed loop control
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| P0746 |
Pressure Control Solenoid "A" Performance/Stuck Off |
OR
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- PWM hardware detection 0 or 100 %
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- low side and high side FET activated
- power supply > 8.7 V
- voltage drop at FET <= 1 V
- solenoid supply > 8.7 V
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| P0747 |
Pressure Control Solenoid "A" Stuck On |
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- PWM hardware detection 0 or 100 %
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- low side and high side FET activated
- power supply > 8.7 V
- voltage drop at FET <= 1 V
- solenoid supply > 8.7 V
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| P0748 |
Pressure Control Solenoid "A" Electrical |
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- current higher or lower > than threshold (50 + 170) mA
OR
- EDS output voltage ~ 0.5 V smaller than EDS supply voltage at short to ground or open circuit
OR
- static leakage current flow
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| P0776 |
Pressure Control Solenoid "B" Performance/Stuck Off |
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- PWM hardware detection 0 or 100 %
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- low side and high side FET activated
- power supply > 8.7 V
- voltage drop at FET <= 1 V
- solenoid supply > 8.7 V
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| P0777 |
Pressure Control Solenoid "B" Stuck On |
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- PWM hardware detection 0 or 100 %
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- low side and high side FET activated
- power supply > 8.7 V
- voltage drop at FET <= 1 V
- solenoid supply > 8.7 V
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| P0778 |
Pressure Control Solenoid "B" Electrical |
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- EDS output voltage ~ 0.5 V smaller than EDS supply voltage at short to ground or open circuit
OR
- static leakage current flow
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| P0779 |
Pressure Control Solenoid "B" Intermittent |
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- PWM hardware detection 0 or 100 %
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- low side and high side FET activated
- power supply > 8.7 V
- voltage drop at FET <= 1 V
- solenoid supply > 8.7 V
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| P0781 |
1-2 Shift |
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DURING GEAR-SHIFT IN PROCESS: (Upshift)
- (input-speed / output-speed) > (start-ratio + ([ 50; 75; 120; 200; 330; 520; 800; 1200] [ 12.44; 9.09; 6.74; 5.16; 4.77; 4.56; 4.42; 4.335] + [ 50; 150; 300; 500; 750; 1100; 1500; 2000] [ 7.6; 4.5; 2.5; 1.15; 0.6; 0.32; 0.15; 0.035]))
AND
- (input-speed / output-speed) < (target-ratio - ([ 140; 200; 360; 570; 870; 1200; 1700; 2300] [ 0; 1.38; 1.79; 2; 2.11; 2.175; 2.222; 2.252] + [ 150; 215; 375; 500; 800; 1200; 1600; 2000] [ 0; 0.77; 0.7; 0.6; 0.44; 0.35; 0.3; 0.26]))
- no monitoring
DURING GEAR-SHIFT IN PROCESS: (Downshift)
- (input-speed / output-speed) < (start-ratio - ([ 140; 200; 360; 570; 870; 1200; 1700; 2300] [ 0; 1.38; 1.79; 2; 2.11; 2.175; 2.222; 2.252] + [ 160; 200; 500; 700; 1000; 1500; 2000; 2400] [ 0; 0.9; 0.9; 0.82; 0.58; 0.39; 0.29; 0.25]))
AND
- and (input-speed / output-speed) > (target-ratio + ([ 50; 75; 120; 200; 330; 520; 800; 1200] [ 12.44; 9.09; 6.74; 5.16; 4.77; 4.56; 4.42; 4.335] + [ 50; 60; 100; 250; 400; 600; 900; 1700] [ 14; 10; 6.2; 1.6; 0.98; 0.66; 0.44; 0.18]))
- no monitoring
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- timer < 0.5 s
- if output-speed >= 50 RPM
- if output-speed < 50 RPM
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- 3 failed rationality checks
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| P0782 |
2-3 Shift |
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DURING GEAR-SHIFT IN PROCESS:
- (input-speed / output-speed) > (start-ratio + ([ 50; 110; 200; 360; 630; 1000; 1500; 2300] [ 9.64; 5.27; 3.32; 2.9; 2.65; 2.54; 2.475; 2.427] + [ 50; 100; 300; 500; 800; 1200; 1800; 3000] [ 10.36; 4.9; 2.3; 1.1; 0.55; 0.29; 0.135; 0.045]))
- and (input-speed / output-speed) < (target-ratio - ([ 180; 200; 380; 650; 1100; 1700; 2500; 3500] [ 0; 0.58; 1; 1.22; 1.34; 1.405; 1.442; 1.465] + [ 50; 320; 500; 800; 1300; 1800; 2300; 3000] [ 0; 0.4; 0.55; 0.5; 0.44; 0.42; 0.38; 0.34]))
- no monitoring
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- timer < 0.5 s
- if output-speed >= 50 RPM
- if output-speed < 50 RPM
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- 3 failed rationality checks
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| P0782 |
2-3 Shift |
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DURING GEAR-SHIFT IN PROCESS:
- (input-speed / output-speed) < (start-ratio - ([ 180; 200; 380; 650; 1100; 1700; 2500; 3500] [ 0; 0.58; 1; 1.22; 1.34; 1.405; 1.442; 1.465] + [ 300; 500; 700; 1000; 1200; 1600; 2000; 3000] [ 0.45; 0.52; 0.65; 0.58; 0.5; 0.39; 0.31; 0.21]))
- and (input-speed / output-speed) > (target-ratio + ([ 50; 110; 200; 360; 630; 1000; 1500; 2300] [ 9.64; 5.27; 3.32; 2.9; 2.65; 2.54; 2.475; 2.427] + [ 50; 80; 140; 300; 500; 1000; 1800; 3000] [ 12; 7; 5; 0.88; 0.5; 0.24; 0.11; 0.045]))
- no monitoring
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- if output-speed >= 50 RPM
- if output-speed < 50 RPM
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- 3 failed rationality checks
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| P0783 |
3-4 Shift |
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DURING GEAR-SHIFT IN PROCESS:
- (input-speed / output-speed) > (start-ratio + ([ 50; 115; 200; 380; 620; 1100; 1900; 3500] [ 8.64; 4.15; 2.45; 2.05; 1.84; 1.705; 1.625; 1.578] + [ 50; 110; 300; 500; 800; 1500; 2500; 5000] [ 7.5; 3.2; 1.5; 0.75; 0.33; 0.18; 0.1; 0.03]))
- and (input-speed / output-speed) < (target-ratio - ([ 180; 290; 500; 800; 1300; 2000; 2800; 4300] [ 0; 0.47; 0.74; 0.895; 0.99; 1.04; 1.072; 1.096] + [ 700; 1000; 1500; 2000; 2500; 3000; 4000; 5000] [ 0.14; 0.15; 0.2; 0.2; 0.18; 0.17; 0.145; 0.12]))
- no monitoring
|
|
- timer < 0.5 s
- if output-speed >= 50 RPM
- if output-speed < 50 RPM
|
- 3 failed rationality checks
|
|
| P0783 |
3-4 Shift |
|
DURING GEAR-SHIFT IN PROCESS:
- (input-speed / output-speed) < (start-ratio - ([ 180; 290; 500; 800; 1300; 2000; 2800; 4300] [ 0; 0.47; 0.74; 0.895; 0.99; 1.04; 1.072; 1.096] + [ 700; 1000; 1500; 2000; 2500; 3000; 4000; 5000] [ 0.4; 0.52; 0.395; 0.31; 0.255; 0.225; 0.18; 0.15]))
- and (input-speed / output-speed) > (target-ratio + ([ 50; 115; 200; 380; 620; 1100; 1900; 3500] [ 8.64; 4.15; 2.45; 2.05; 1.84; 1.705; 1.625; 1.578] + [ 50; 400; 700; 1000; 1500; 2000; 3000; 5000] [ 7; 1.5; 0.7; 0.4; 0.25; 0.2; 0.13; 0.06]))
- no monitoring
|
|
- if output-speed >= 50 RPM
- if output-speed < 50 RPM
|
- 3 failed rationality checks
|
|
| P0784 |
4-5 Shift |
|
DURING GEAR-SHIFT IN PROCESS:
- (input-speed / output-speed) > (start-ratio + ([ 50; 100; 200; 370; 650; 1200; 2300; 4300] [ 8.52; 4.02; 2.12; 1.68; 1.45; 1.305; 1.23; 1.189] + [ 50; 500; 900; 1500; 2000; 3000; 5000; 6000] [ 7; 0.8; 0.4; 0.2; 0.11; 0.06; 0.035; 0.019]))
- and (input-speed / output-speed) < (target-ratio - ([ 220; 350; 600; 1000; 1500; 2300; 3500; 5000] [ 0; 0.31; 0.55; 0.67; 0.735; 0.78; 0.81; 0.828] + [ 1100; 1250; 1500; 2000; 3000; 4000; 5000; 6000] [ 0.27; 0.25; 0.23; 0.2; 0.15; 0.12; 0.1; 0.08]))
- no monitoring
OR
- (input-speed / output-speed) < (start-ratio - ([ 220; 350; 600; 1000; 1500; 2300; 3500; 5000] [ 0; 0.31; 0.55; 0.67; 0.735; 0.78; 0.81; 0.828] + [ 1100; 1500; 1750; 2000; 3000; 4000; 5000; 6000] [ 0.3; 0.38; 0.33; 0.29; 0.2; 0.15; 0.12; 0.095]))
- and (input-speed / output-speed) > (target-ratio + ([ 50; 100; 200; 370; 650; 1200; 2300; 4300] [ 8.52; 4.02; 2.12; 1.68; 1.45; 1.305; 1.23; 1.189] + [ 50; 500; 900; 1500; 2000; 3000; 5000; 6000] [ 7.5; 0.5; 0.26; 0.15; 0.11; 0.07; 0.04; 0.02]))
- no monitoring
|
|
- timer < 0.5 s
- if output-speed >= 50 RPM
- if output-speed < 50 RPM
|
- 3 failed rationality checks
|
|
| P0796 |
Pressure Control Solenoid "C" Performance/Stuck Off |
- short to ground, open circuit
|
- PWM hardware detection 0 or 100 %
|
|
- low side and high side FET activated
- power supply > 8.7 V
- voltage drop at FET <= 1 V
- solenoid supply > 8.7 V
|
|
|
| P0797 |
Pressure Control Solenoid "C" Stuck On |
|
- PWM hardware detection 0 or 100 %
|
|
- low side and high side FET activated
- power supply > 8.7 V
- voltage drop at FET <= 1 V
- solenoid supply > 8.7 V
|
|
|
| P0798 |
Pressure Control Solenoid "C" Electrical |
|
- current higher or lower than threshold < (850 - 120) mA
|
|
|
|
|
|
|
- EDS output voltage at short to ground or open circuit ~ 0.5 V smaller than EDS supply voltage
|
|
- static leakage current flow
|
|
| P0829 |
5-6 Shift |
|
DURING GEAR-SHIFT IN PROCESS:
- (input-speed / output-speed) > (start-ratio + ([ 50; 100; 200; 400; 750; 1400; 2700; 5000] [ 8.71; 3.75; 1.82; 1.36; 1.13; 1.007; 0.94; 0.907] + [ 50; 900; 1500; 2000; 3000; 4000; 5000; 7000] [ 7.5; 0.35; 0.2; 0.14; 0.08; 0.05; 0.04; 0.01]))
- and (input-speed / output-speed) < (target-ratio - ([ 300; 380; 500; 750; 1300; 2200; 3700; 6000] [ 0; 0.19; 0.29; 0.43; 0.54; 0.602; 0.638; 0.658] + [ 1500; 2000; 2500; 3000; 4000; 5000; 6000; 7000] [ 0.27; 0.25; 0.2; 0.165; 0.13; 0.108; 0.095; 0.08]))
- no monitoring
OR
- (input-speed / output-speed) < (start-ratio - ([ 300; 380; 500; 750; 1300; 2200; 3700; 6000] [ 0; 0.19; 0.29; 0.43; 0.54; 0.602; 0.638; 0.658] + [ 1500; 2000; 2500; 3000; 4000; 5000; 6000; 7000] [ 0.28; 0.27; 0.24; 0.21; 0.16; 0.13; 0.11; 0.09]))
- and (input-speed / output-speed) > (target-ratio + ([ 50; 100; 200; 400; 750; 1400; 2700; 5000] [ 8.71; 3.75; 1.82; 1.36; 1.13; 1.007; 0.94; 0.907] + [ 50; 180; 490; 900; 2000; 3500; 5500; 7000] [ 8; 3; 0.9; 0.38; 0.17; 0.1; 0.055; 0.026]))
- no monitoring
|
|
- timer < 0.5 s
- if output-speed >= 50 RPM
- if output-speed < 50 RPM
|
- 3 failed rationality checks
|
|
| P0889 |
TCM Power Relay Sense Circuit Range/Performance |
|
|
|
- filtered battery voltage > 6.75 V
- high side and low side FET activated
- status counter initialization 0 or 1
|
|
|
| P0890 |
TCM Power Relay Sense Circuit Low |
|
- solenoid power supply voltage < 1.4 V
- drop voltage over High Side FET > 1 V
|
|
- filtered battery voltage > 6.75 V
- high side and low side FET activated
- status counter initialization 0 or 1
|
|
|
| P0891 |
TCM Power Relay Sense Circuit High |
|
|
|
- filtered battery voltage > 6.75 V
- high side and low side FET activated
- status counter initialization 0 or 1
|
|
|
| P0892 |
TCM Power Relay Sense Circuit Intermittent |
|
|
|
- filtered battery voltage > 6.75 V
- high side and low side FET activated
- status counter initialization 0 or 1
|
|
|
| P1703 |
Limp home, control unit reset |
|
POWERFLOW DETECTED AFTER RESET:
- engine speed > 500 RPM
- output speed < 50 RPM
- position lever R or D or S
- break paddle not pressed
|
|
|
|
|
| P2637 |
Torque Management Feedback Signal "A" |
|
- CAN message signal error flag = 1
|
|
- ignition On
- CAN Bus no error detected
- ECM CAN connection no error detected
- battery voltage > 9 V
|
|
|
| P2700 |
Transmission Friction Element "A" Apply Time Range/Performance |
|
- (input-speed / output-speed) > [ 50; 110; 200; 360; 630; 1000; 1500; 2300] [ 9.64; 5.27; 3.32; 2.9; 2.65; 2.54; 2.475; 2.427]
- gear ratio = input-speed / output-speed
OR
- (input-speed / output-speed) < [ 140; 200; 360; 570; 870; 1200; 1700; 2300] [ 0; 1.38; 1.79; 2; 2.11; 2.175; 2.222; 2.252]
- (output-speed x ratio - input-speed) > 320 RPM
|
|
- oil-temperature > 0° C
- engine speed > 400 RPM
- input speed > 0 RPM
- input speed no error detected
- gear position not (P or N or NIC)
- timer < 0.5 s
- if output-speed >= 50 RPM
- if output-speed < 50 RPM
|
- 3 failed rationality checks
|
|
| P2701 |
Transmission Friction Element "B" Apply Time Range/Performance |
|
- Explanation: [X1;X2;XN] [Y1;Y2;YN]
- at X is equal Y
- X correspond to output-speed RPM
- Y correspond to gear ratio
- gear ratio = input-speed / output-speed
(OUT OF GEAR-SHIFT TIMER AND GEAR-ENGAGEMENT)
- (input-speed / output-speed) > [ 50; 115; 200; 380; 620; 1100; 1900; 3500] [ 8.64; 4.15; 2.45; 2.05; 1.84; 1.705; 1.625; 1.578]
- or (input-speed / output-speed) < [ 180; 200; 380; 650; 1100; 1700; 2500; 3500] [ 0; 0.58; 1; 1.22; 1.34; 1.405; 1.442; 1.465]
- (output-speed x ratio - input-speed) > 320 RPM
OR
- (input-speed / output-speed) > [ 50; 100; 200; 400; 750; 1400; 2700; 5000] [ 8.71; 3.75; 1.82; 1.36; 1.13; 1.007; 0.94; 0.907]
- or (input-speed / output-speed) < [ 220; 350; 600; 1000; 1500; 2300; 3500; 5000] [ 0; 0.31; 0.55; 0.67; 0.735; 0.78; 0.81; 0.828]
- (output-speed x ratio - input-speed) > 320 RPM
OR
- (input-speed / output-speed) < [ 140; 200; 360; 570; 870; 1200; 1700; 2300] [ 0; 1.38; 1.79; 2; 2.11; 2.175; 2.222; 2.252]
- (output-speed x ratio - input-speed) > 320 RPM
|
|
GENERAL ENABLE REQUIREMENTS:
- oil-temperature > 0 [°C]
- engine speed > 400 RPM
- input speed > 0 RPM
- input speed no error detected
- gear position not (P or N or NIC)
- timer < 0.5 s
- if output-speed >= 50 RPM
- if output-speed < 50 [RPM
|
- 3 failed rationality checks
|
|
| P2702 |
Transmission Friction Element "C" Apply Time Range/Performance |
|
- (input-speed / output-speed) > [ 50; 110; 200; 360; 630; 1000; 1500; 2300] [ 9.64; 5.27; 3.32; 2.9; 2.65; 2.54; 2.475; 2.427]
- gear ratio = input-speed / output-speed
OR
- (input-speed / output-speed) < [ 140; 200; 360; 570; 870; 1200; 1700; 2300] [ 0; 1.38; 1.79; 2; 2.11; 2.175; 2.222; 2.252]
- (output-speed x ratio - input-speed) > 320 RPM
|
|
- oil-temperature > 0° C
- engine speed > 400 RPM
- input speed > 0 RPM
- input speed no error detected
- gear position not (P or N or NIC)
- timer < 0.5 s
- if output-speed >= 50 RPM
- if output-speed < 50 RPM
|
- 3 failed rationality checks
|
|
| P2703 |
Transmission Friction Element "D" Apply Time Range/Performance |
|
- (output-speed x ratio - input-speed)
|
|
- oil-temperature > 0° C
- engine speed > 400 RPM
- input speed > 0 RPM
- input speed no error detected
- gear position not (P or N or NIC)
- timer < 0.5 s
- if output-speed >= 50 RPM
- if output-speed < 50 RPM
|
- 3 failed rationality checks
|
|
| P2704 |
Transmission Friction Element "E" Apply Time Range/Performance |
|
- Explanation: [X1;X2;XN] [Y1;Y2;YN]
- at X is equal Y
- X correspond to output-speed RPM
- Y correspond to gear ratio
- gear ratio = input-speed / output-speed
(OUT OF GEAR-SHIFT TIMER < 0.5 [S] AND GEAR-ENGAGEMENT)
- (input-speed / output-speed) > [ 50; 100; 200; 370; 650; 1200; 2300; 4300] [ 8.52; 4.02; 2.12; 1.68; 1.45; 1.305; 1.23; 1.189]
- or (input-speed / output-speed) < [ 180; 290; 500; 800; 1300; 2000; 2800; 4300] [ 0; 0.47; 0.74; 0.895; 0.99; 1.04; 1.072; 1.096]
- (output-speed x ratio - input-speed) > 320 RPM
OR
- (input-speed / output-speed) < [ 140; 200; 360; 570; 870; 1200; 1700; 2300] [ 0; 1.38; 1.79; 2; 2.11; 2.175; 2.222; 2.252]
- (output-speed x ratio - input-speed) > 320 RPM
OR
- (input-speed / output-speed) > [ 50; 200; 340; 600; 1000; 1800; 3300; 6000] [ 7.74; 1.68; 1.27; 1.03; 0.885; 0.8; 0.752; 0.724]
- or (input-speed / output-speed) < [ 300; 380; 500; 750; 1300; 2200; 3700; 6000] [ 0; 0.19; 0.29; 0.43; 0.54; 0.602; 0.638; 0.658]
- (output-speed x ratio - input-speed) > 320 RPM
|
|
GENERAL ENABLE REQUIREMENTS:
- oil-temperature > 0° C
- engine speed > 400 RPM
- input speed > 0 RPM
- input speed no error detected
- gear position not (P or N or NIC)
- timer < 0.5 s
- if output-speed >= 50 RPM
- if output-speed < 50 RPM
|
- 3 failed rationality checks
|
|
| P2714 |
Pressure Control Solenoid "D" Performance/Stuck Off |
- short to ground, open circuit
|
- PWM hardware detection 0 or 100 %
|
|
- low side and high side FET activated
- power supply > 8.7 V
- voltage drop at FET <= 1 V
- solenoid supply > 8. V
|
|
|
| P2715 |
Pressure Control Solenoid "D" Stuck On |
|
- PWM hardware detection 0 or 100 %
|
|
- low side and high side FET activated
- power supply > 8.7 V
- voltage drop at FET <= 1 V
- solenoid supply > 8. V
|
|
|
| P2716 |
Pressure Control Solenoid "D" Electrical |
|
- current higher or lower than threshold > (50 + 170) [mA]
|
|
|
|
|
|
|
- EDS output voltage at short to ground or open circuit ~ 0.5 V smaller than EDS supply voltage
|
|
- static leakage current flow
|
|
| P2723 |
Pressure Control Solenoid "E" Performance/Stuck Off |
- short to ground, open circuit
|
- PWM hardware detection 0 or 100 %
|
|
- low side and high side FET activated
- power supply > 8.7 V
- voltage drop at FET <= 1 V
- solenoid supply > 8. V
|
|
|
| P2724 |
Pressure Control Solenoid "E" Stuck On |
|
- PWM hardware detection 0 or 100 %
|
|
- low side and high side FET activated
- power supply > 8.7 V
- voltage drop at FET <= 1 V
- solenoid supply > 8.7 V
|
|
|
| P2725 |
Pressure Control Solenoid "E" Electrical |
|
- current higher or lower than threshold > (50 + 170) [mA]
|
|
|
|
|
|
|
- EDS output voltage at short to ground or open circuit ~ 0.5 V smaller than EDS supply voltage
|
|
- static leakage current flow
|
|
| P2732 |
Pressure Control Solenoid "F" Performance/Stuck Off |
- short to ground, open circuit
|
- PWM hardware detection 0 or 100 %
|
|
- low side and high side FET activated
- power supply > 8.7 V
- voltage drop at FET <= 1 V
- solenoid supply > 8. V
|
|
|
| P2733 |
Pressure Control Solenoid "F" Stuck On |
|
- PWM hardware detection 0 or 100 %
|
|
- low side and high side FET activated
- power supply > 8.7 V
- voltage drop at FET <= 1 V
- solenoid supply > 8.7 V
|
|
|
| P2734 |
Pressure Control Solenoid "F" Electrical |
|
- current higher or lower than threshold > (50 + 170) [mA]
|
|
|
|
- 2 DCY
- continuous
- low side FET activated
|
|
|
- EDS output voltage at short to ground or open circuit ~ 0.5 V smaller than EDS supply voltage
|
|
- static leakage current flow
|
|
| P2814 |
Pressure Control Solenoid "G" Control Circuit Low |
|
- if PWM = 0% diagnosis by ASIC
- if 0% <= PWM < 7.6%
- voltage return lead (low) < 0.75 [V
- if 7.6% <= PWM <= 92.4%
- voltage return lead (high) < 0.75 V
- and voltage return lead (low) < 0.75 V
|
|
- high side FET voltage drop <= 1 V
- high side FET activated
- low side FET activated
|
|
|
| U0001 |
High Speed CAN Communication Bus |
|
- CAN IC internal diagnostics
- detects CAN Bus off
- no CAN Bus activity
|
|
- battery voltage > 9 V
- battery voltage < 16. V
- delay after ignition on 0.5 s
|
|
|
|
|
|
|
| U0100 |
Lost Communication With ECM/PCM "A" |
|
- no message received from ECM timeout
|
|
- CAN Bus no error and ready to transmit
- delay after ignition on 1 s
- battery voltage > 9 V
|
|
|
|
|
|
| U0302 |
Software Incompatibility With Transmission Control Module |
|
- wrong calibration data incorrect
|
|
|
|
|
| U0401 |
Invalid Data Received From ECM/PCM "A" |
|
|
|
- CAN Bus no error and ready to transmit
- delay after ignition on 1 s
- battery voltage > 9 V
|
|
|